SS Marine Sulphur Queen - Investigation

Investigation

A Coast Guard investigation concluded several facts about the Marine Sulphur Queen which, by themselves, should have prevented the ship from going to sea at all. The most important were the incidents of fire beneath and along the sides of the four large sulphur tanks; according to former crewmen these fires were so common that ship's officers gave up sounding the fire alarm. On one occasion the ship sailed into a New Jersey harbor, off-loaded cargo, and sailed out with a fire still burning. When a fire was actually put out, the sulphur would puddle and cake around equipment, once shorting out a major electrical generator. Caked sulphur was also found in spaces below the tanks, due to many cracks in the structure.

The Coast Guard also noted that the T2 tanker class had a characteristic "weak back", meaning the keel would split at a point weakened by corrosion, usually around midships. Such a splitting had happened on several T2 tankers, and many were discovered during inspections to have hairline or larger fractures within the keel and on major frames. Companies who owned T2 tankers were ordered to pay attention to the keel when inspecting. Former crewmen also testified that corrosion was everywhere, mentioning inoperable temperature gauges, a ruptured steam coil, and worn packing around the screws. It was recorded that Marine Sulphur Queen was scheduled for a drydock inspection in January 1963, but it was postponed by the owners, who had complained that cargo deliveries were behind and they needed their ships to catch up. One new crewman, on reporting to the ship just before it sailed for the last time, turned to his wife and pronounced it "a floating garbage can."

In the closing of the inquiry, it came as no surprise that the Coast Guard had this to say:

1. In view of the vast search operations conducted and the debris found and identified as coming from the MARINE SULPHUR QUEEN, the ship and her entire crew of 39 men are presumed to be lost.
2. Concurring with the Board, the vessel apparently was lost on 4 February 1963 on its approach to, or in the vicinity of, the Straits of Florida.
3. Further concurring with the Board, in the absence of survivors or physical remains of the ship, the exact cause of the loss of the MARINE SULPHUR QUEEN cannot be determined.
4. The Board considered many possibilities which may have caused the loss of the ship and rightly declined to assign any order of probability to these causes. In its conclusions the Board commented on the following possible causes:
a. An explosion may have occurred in the cargo tanks.
b. A complete failure of the vessel's hull girder may have caused it to break in two
c. The vessel may have capsized in synchronous rolling
d. A steam explosion may have occurred as the result of a rapid filling of the void space with water.
The record contains ample evidence to support the Board's suppositions.

The Coast Guard also recommended that no remaining T2 tanker be converted into a sulphur carrier without taking into consideration the structure of the ship as originally built. "First, the acceptability of any conversion must be considered on its individual merits, having regard for the existing condition of the vessel and the proposed cargo, route, and service. Secondly, the objection to the conversion of an existing T2 or another tanker of comparable age is associated with the probable condition of the vessel, particularly the cargo portion, due to age, as much as it is due to design considerations."

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